Orbiter Lh2 Feedline Flowliner Cracking Problem; Version 1.0 Buy on Amazon

https://www.ebooknetworking.net/books_detail-1287253849.html

Orbiter Lh2 Feedline Flowliner Cracking Problem; Version 1.0

PublisherBiblioGov
20.75 USD
Buy New on Amazon 🇺🇸 Buy Used — $15.37

Usually ships in 24 hours

Book Details

PublisherBiblioGov
ISBN / ASIN1287253849
ISBN-139781287253846
AvailabilityUsually ships in 24 hours
Sales Rank99,999,999
MarketplaceUnited States  🇺🇸

Description

In May of 2002, three cracks were found in the downstream flowliner at the gimbal joint in the LH2 feedline at the interface with the Low Pressure Fuel Turbopump (LPFP) of Space Shuttle Main Engine (SSME) #1 of Orbiter OV-104. Subsequent inspections of the feedline flowliners in the other orbiters revealed the existence of 8 additional cracks. No cracks were found in the LO2 feedline flowliners. A solution to the cracking problem was developed and implemented on all orbiters. The solution included weld repair of all detectable cracks and the polishing of all slot edges to remove manufacturing discrepancies that could initiate new cracks. Using the results of a fracture mechanics analysis with a scatter factor of 4 on the predicted fatigue life, the orbiters were cleared for return to flight with a one-flight rationale requiring inspections after each flight. OV-104 flew mission STS-112 and OV-105 flew mission STS-113. The post-flight inspections did not find any cracks in the repaired flowliners. At the request of the Orbiter Program, the NESC conducted an assessment of the Orbiter LH2 Feedline Flowliner cracking problem with a team of subject matter experts from throughout NASA.

More Books by Charles E. Harris

Donate to EbookNetworking
Prev
Next