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Laboratory Investigation of Two Autopilots for a 4/10-Scale Drop Model of the Grumman F8f-1 Airplane, Ted No. NACA 2466

Author Jerome M. Teitelbaum, Ernest C. Seaberg
Publisher BiblioGov
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Book Details
PublisherBiblioGov
ISBN / ASIN1289260796
ISBN-139781289260798
AvailabilityUsually ships in 24 hours
Sales Rank99,999,999
MarketplaceUnited States 🇺🇸

Description

Performance investigation and frequency response analyses were con- ducted en two autopilot control systems designed for use in the 0.4-scale model of the Grumman F8F-1 airplane. The first system, based on the action of a displacement gyroscope only, was investigated to find the cause of a small-amplitude pitch oscillation which had been noted in previous flight tests. The results of the investigation conducted revealed that, although the autopilot-model combination was dynamically stable, a hunting oscillation was possible due to a change in autopilot characteristics in a dive. This hunting condition can be eliminated by increasing the gyroscope pickoff dead spot without greatly reducing dynamic stability of the autopilot-model combination.